this post was submitted on 07 Jan 2024
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My assumption is that the 737 Max is simply a fundamentally unsafe and unsound design.
I'm sure within 15 years they'll complete the final retrofit to make it safe and sound, and in the end, it will end up costing 300% of what a new design would have.
But, it'll actually work out for Boeing executives and shareholders, so it will be taught to future MBA student as a success story about the heroic and stoic leadership that generated record profits for the low cost of a few hundred lives.
Most of the fuselage should be insanely similar to other 737 models. I can't imagine how someone fucked up badly enough to lose a door plug,
That's the problem... Reusing a 50+-year-old design, with new engines and other technology that should have been used with a new fuselage design...
I don't think they'd ground the entire fleet if this was just a mechanic who made some one-off error. There's probably some human error involved, but those on the ground human errors are only catastrophic because of the design choices Boeing made.
I mean I'd argue it's only 30 years since NG, but that's a different argument. It's not like it isn't a proven airframe that still goes through continual process improvements. They certainly could have done things differently, but way more time and cost.
I don't think they know the exact cause and they grounded them out of an excess of caution. I'm going to guess a process got bought off that wasn't complete. That's the kind of thing that's engineered to not fall off if it's properly installed.
We'll see how things pan out in the next few days.